Recently I tried the Chuck to ARM project on Pluto X and runs successfully. After that I Tried the Turtle Turn project, and the code is flashed successfully and connected to the Application but the drone is not performing the desired task. After that I changing to motor connection to M6-M8, but the drone propeller is still not responding. In application drone still connected but no operation even in non developer mode.
Hello nitesh , from your pluto controller app go into update firmware and flash pluto x firmware which will reset the drone and then try doing your project again